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Cebora SOUND MIG 5040/T D Manual De Instrucciones página 17

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Idiomas disponibles

Idiomas disponibles

CEBORA S.p.A.
45
Push-pull board not connected.
(only 289)
46
Push-pull board error.
(only 289)
"trG"
Start
button
(53)
overtemperature alarm reset.
Output current presence at the Power
54
Source start up (short circuit between
torch and workpiece).
Time-out max. Short circuit lasting time
56
excessive.
"Mot"
Excessive error Wire Feeder Motor
(57)
current.
58
Firmware versions misalignment error.
(only 289)
L1 Mains Phase voltage lower than
61
minimum allowed value.
62
L1 Mains Phase voltage higher than
(only 289)
maximum allowed value.
63
L2 Mains Phase voltage lower than
(only 289)
minimum allowed value.
64
L2 Mains Phase voltage higher than
(only 289)
maximum allowed value.
65
L3 Mains Phase voltage lower than
(only 289)
minimum allowed value.
66
L3 Mains Phase voltage higher than
(only 289)
maximum allowed value.
"tH0"
Output Diodes overtemperature.
(73)
"tH1"
Inverter Igbt overtemperature (analogue
(74)
signal).
"H2O"
Cooling liquid pressure low.
(75)
"Opn"
Wire Feeder Motor carter open.
(80)
"rob"
Emergency stop by Robot, or Robot off.
90
"Sti"
Stuck wire.
(91)
"End"
Wire end.
(92)
"Ito"
Inching time out.
(98)
"OFF"
Mains supply missing (Power Source
(99)
power off).
3.300.160-F
Check wiring between Push-pull and Motor Control
boards. Replace Push-pull and/or Motor Control boards.
Check wiring between Push-pull and Motor Control
boards. Replace Push-pull and/or Motor Control boards.
pressed
at
the
Replace Connector and/or Motor Control boards.
Check the power wiring between output Diode Group and
Power Source output terminals. Replace Control board
and/or Current Transducer.
Check torch wearing conditions, power wiring between
Diode Group and Power Source output terminals. Replace
Measurement and/or Control and/or Driver-ac boards
and/or Current Transducer.
Replace Wire Feeder Motor or Wire Feeder group and/or
Motor Control board.
Re-Program Power Source with the right firmware
versions. Replace Control and/or Motor Control and/or
Panel boards.
Make sure the mains three phases values. Replace
Precharge and/or Control boards.
Make sure the mains three phases values. Replace
Precharge and/or Control boards.
Make sure the mains three phases values. Replace
Precharge and/or Control boards.
Make sure the mains three phases values. Replace
Precharge and/or Control boards.
Make sure the mains three phases values. Replace
Precharge and/or Control boards.
Make sure the mains three phases values. Replace
Precharge and/or Control boards.
Replace Thermostat on Diode Group and/or Control
board.
Replace Thermostat board on Igbt Group and/or Control
board.
Check the wired bridge presence on terminals 3 and 4 of
connector J18 Control board (only 289). Replace pressure
switch on cooling unit and/or Precharge and/or Control
boards. Replace Control Board.
Replace carter switch and/or Motor Control board.
Check Power Source - Robot connections and Robot
power supply and/or plant safety conditions.
Cut the wire or perform the "automatic wire detachment
procedure" (see Robot Interface Instructions Manual).
Replace the wire spool.
Replace Control board.
Replace Precharge and/or Control board.
17
GB
10-03-2016

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