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Cebora MIG3240/T Manual De Instrucciones página 17

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Idiomas disponibles

Idiomas disponibles

CEBORA S.p.A.
Excessive error Wire Feeder Motor
57
current.
Firmware
58
error.
Mains voltage lower than minimum
61
allowed value.
"tH0"
Output Inverter Igbt or Diodes
(73)
Group overtemperature.
"H2O"
Cooling liquid pressure low.
(75)
"nc"
Cooling Unit not connected.
(76)
"
"
GAS LO
Gas low pressure.
(78)
"
"
GAS HI
Gas high pressure.
(79)
"OPn"
Wire Feeder Motor carter open.
(80)
"GAS nc"
GAS Sensor not connected.
(81)
"QC"
"Quality Control" test failed.
(84)
"rob"
Emergency stop by Robot, or Robot
(90)
off.
"Sti"
Stuck wire.
(91)
"End"
Wire end.
(92)
"Ito"
Inching time out.
(98)
"OFF"
Mains
supply
(99)
Source power off).
3.300.208-A
versions
misalignment
missing
(Power
Replace Wire Feeder Motor or Wire Feeder group
and/or Motor Control board.
Re-Program Power Source with the right firmware
versions. Replace Control and/or Motor Control and/or
Control Panel boards.
Make sure the mains three phases values. Replace
Precharge and/or Control boards.
Replace thermostat on Inverter Igbt or Diodes Group
and/or Control board.
Check the wiring between Control board and connector
BN on the Power Source back panel.
Replace pressure switch on Cooling Unit.
Check wiring between Cooling Unit and Power Source.
In case of Cooling Unit missing, check the right plug
connection on BN connector on Power Source rear
panel.
Check the real gas pressure. Check the connections of
Gas Sensor with the Motor Control board.
Replace Motor Control board and/or Gas Sensor.
Check the real gas pressure. Check the connections of
Gas Sensor with the Motor Control board.
Replace Motor Control board and/or Gas Sensor.
Replace carter switch and/or Motor Control board.
Check connections of the Gas Sensor with the Motor
Control board, and the presence of Jumper 11 on the
J10 strip on Motor Control board (see Kit Gas Sensor
Instructions Manual).
Replace Motor Control board and/or Gas Sensor.
Not operative.
Check Power Source - Robot connections and Robot
power supply and/or plant safety conditions.
Cut the wire or perform the "automatic wire
detachment
procedure"
Instructions Manual).
Replace the wire spool.
Replace Control board.
Replace Precharge and/or Control boards.
17
(see
Robot
Interface
04-03-2016
GB

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